Last
week we finished up some minor electrical connections, such as the green
neutral lights on the shifters and the transmission pressure gauges – although
they’ll need new sending units to register correctly. We ran both engines
at between 1500 and 2000 rpm until they both came up to temperature so the
thermostats would open and circulate coolant to wherever it needed to go.
We added some coolant to the starboard engine to compensate for the long lines
running to our hot water tank and back.
When we did the first
start a few days prior, we noticed a puff of smoke from the port engine when it
first started. It did that again, and with it running for 30 or 40
minutes we could notice a definite exhaust leak smell, even though there wasn’t
much smoke. Further examination the next day, after all had cooled off,
revealed a leak between the turbocharger and the exhaust riser. We
tightened those bolts in the hope that they weren’t quite tight enough, but that
didn’t improve the situation at all.
We decided to disconnect
the riser, which required removing the insulating blanket as well as the raw
water hose to the injection elbow. What was revealed was that the flange
of the turbocharger was in no shape to support a good seal to the flange of the
riser. It was pitted and corroded to the extent that the ridge on the
metal compression gasket did not fully engage with the housing.
Our
choices as to fixing it seemed to be to either machine the housing down to a
flat surface, or replace the turbocharger. Mechanically, the turbocharger
was fine, spinning freely with no bearing play at all, but I wasn’t too keen on
the machining, as it appeared that the pitting was caused by water damage
in a previous lifetime for this unit and there may be other issues inside
waiting for us. Also, the amount we’d have to take off to square it up
would reduce the bolt hole depth and thus weaken the connection to the
riser. I sent photos to Seamaster Marine in Florida, where we purchased
the engines, and they agreed to send up another turbocharger, which should be
on its way today. We’ve removed this one from the boat and will pack it
up and send it back. Unlike the turbochargers on the old Perkins engines,
these units are water cooled, so we had to drain all the coolant from the port
engine – we’ll be going through the thermostat exercise again.
So,
our initial sea trial has been delayed by at least a week while we wait for the
new turbocharger. That’s when we’ll find out if we can reach the engines’
rated maximum rpm of 2600. According to some online calculators we should
be able to, or at least come close. This will tell us if our props are
the right size. If we are substantially below max rpm, we may have to
have the props re-pitched – otherwise the engines could be overloaded even at
the lower rpms.
We
did get the roof panel we removed bolted into place so it wouldn’t go flying
off as we headed into the wind. Patching the saw kerfs will come later,
so our sea trial will be on a dry day – perhaps another unreasonable
requirement this time of year. Irv from Gallery Marine warned us that we
should expect smoke and burning smells from the paint on the engines as
manifolds and other various parts come up to operating temperatures. He
told us that they usually don’t even take customers along on an initial sea
trial run for this reason, adding “whatever you do, don’t bring the womenfolk
along – they always freak out.”
The
turbocharger weighs close to 50 pounds, so Ray made a shipping box for it from
some scrap pieces of plywood and 2x2s.
I'd say this box is pretty well engineered!
Erin
and I did some weekend work at the boat while waiting for our replacement
turbocharger. Our above average rainfall has made an appreciable change
to the lake level, as the boat has risen well over a foot over the last month
or two. So, we brought along the steps that we’ve been bringing home each
fall.
Erin busied herself
polishing chrome while I inflated the dinghy and washed off some of the grime
that has accumulated on the boat – one of the benefits of mooring under the I-5
Ship Canal Bridge. In an attempt to keep water from pouring through the
saw kerfs of our roof hatch and into the salon, I covered the openings with
tape.
For the most part it worked, except for a drip in one corner.
So now we’ll at least look somewhat respectable from a distance when we head out into the lake for sea trials once our replacement
turbocharger arrives. Ray and I recently reconnected the lines to the air
horns, so at Erin’s urging, of course, I gave her a brief demo, being careful
to not signal the University Bridge to open.
While waiting for the
replacement turbo to arrive we set about installing a pair of coolant reservoir
overflow bottles, which I had purchased on Ebay. Just as in your car,
these allow expanding coolant to collect and then draw back into the cooling
system as it cools. The automotive versions of these overflow bottles
come in all shapes and sizes to be tucked into the car’s engine compartment,
but these are universal bottles and needed brackets to secure them. The
engine block had some conveniently placed threaded holes just behind the
expansion tank, and Ray made some steel brackets that we could bolt on there.
Ray is preparing the port
engine to receive the new bracket, which you see in the foreground. He
had to add on the offset piece with another pair of bolt holes, as, unlike the
starboard engine, the port engine had a brace to the expansion tank bolted
there. The kitty litter bucket contains the coolant we drained to remove
the turbocharger.
Our
replacement turbocharger arrived on 3/29, but on that same day Chief Engineer
Ray was ill, and eventually was checked into the hospital for abdominal surgery
to repair a hernia as well as some strangulated bowel. The good news is that Ray has since
recovered, and we delayed any sea trial attempt until he was ready to participate,
hear the roar of the exhaust and smell the paint burning off the manifolds as
we accelerate to maximum rpm out in Lake Washington. It’s a big step in
the fruition of our labors over the past several months.
Here are photos of the old
and replacement turbocharger exhaust housings. The replacement
turbocharger appears to have a brand new housing on the exhaust side. It
had so much more metal on it that I double checked the number in the casting to
make sure it was the same part. While I’m glad they sent the replacement
without question, I’m a bit surprised they let the first one leave the shop.
I
was pretty sure Ray wouldn’t be interested in hefting the 45 lb. turbocharger
anytime soon, so while he was recovering I got it bolted into place. New
gaskets came with it as well, and I added some high-temp silicone sealer
between the manifold and turbo, and some lithium grease to the exhaust
port. Once the turbocharger was securely
in place I could add the coolant back into the engine. Rather than mess with a
funnel and trying to clumsily pour from the bucket into the smaller bottles or
the expansion tank, I found some hose and started a siphon to fill the
engine. It worked great and I poured the individual jugs of coolant into
the bucket as
the level was siphoned
down. You can see the reservoir bottle bolted into place and yes, the
overflow hose has since been connected to it.
With
the exhaust and raw water systems reconnected, and coolant back in the engine I
started it up for a test. No exhaust leaks, and enough coolant found its
way into some additional areas that I could add nearly another gallon to top it
up.
Diesel
engines need to be able to achieve their maximum rated rpm at wide open
throttle under load to assure that they are not overloaded throughout their
working range. In actual use, we will seldom, probably never, run at the
maximum rpm, but if the engines are unable reach their maximum, in this case
2600 rpm, it will mean the boat is “over-propped” – the diameter and pitch of
the propellers take too big of a bite for the engine to handle properly (no pun
intended). While we could easily cruise at our usual 8 or 9 knots even
when over-propped, it could be likened to driving around in a stick shift car
in high gear at 15 or 20 mph – you can do it but it’s not good for the engine
to be lugged down like that. We’ve used calculators available online that
indicate we are pretty close to being just fine based on our horsepower, boat
weight, length, beam, reduction gear ratio, and diameter and pitch of the
propellers. But the real test will be when we head out on the water to
see how she performs. If we end up topping out a couple hundred rpm short
of max, then when we haul the boat out for maintenance we’ll take the props to
the prop shop and tell them we need a couple hundred more rpm. They’ll
know how much pitch needs to be taken out if that’s the case.
With
the engines pretty much ready for sea trials, I decided to focus on some other
chores while Ray recovered from his surgery. As part of opening up the
hatch in the roof we had to cut through some wires as well as the copper tubing
to the air horns. The wires were to the stereo speakers further ahead in
the roof. They are shielded pairs, and required some nipping to get to the individual wires inside. They’ll be
rejoined with compression splices. Ray and I had already reconnected the
horns using plastic tubing, but the tubes needed to be secured so they wouldn’t
cause a bump once we put the headliner back into place.
I had reused the
transmission oil pressure senders for our new gauge configuration, since they
were working in the old configuration. What I didn’t take into account
was the scale on the gauges. The gear pressure gauges on the Perkins
panels ran from 0 to 400 psi. The transmissions actually operated at
pressures between 90 to 130 lbs, and I used new VDO gauges with a 0 – 150 lb
scale. The old sending units work exactly as designed, and for 100 lbs of
pressure they move the needle one fourth of the way through the range – so what
registered as 100 lbs on the old gauges registers as about 35 lbs on the new
gauges. The old sending units were equipped with half inch pipe thread
for attaching to the transmissions. Most of the new sending units use 1/8
pipe thread, although the half inch was available. The problem was that
the same sending unit that cost $24 with 1/8 thread was priced at $56 with half
inch thread. Yikes. I bought the new units with 1/8 thread, and for
68 cents apiece got these threaded bushings to convert them. These will
go on the transmissions in the next day or two, and then the gear pressure
should register correctly.
I continued working on the
boat during Ray's recovery, and noticed there was some fresh fuel in the
bilge. I had been swapping out oil
absorbent pads there ever since the Perkins injector pump had its leak, so I
noticed the new fuel right away. With
the engines running I discovered a fairly significant fuel leak on the
starboard engine. I could see it running down the side of the block and
dripping off the bottom of the engine. I’m pretty sure it wasn’t doing
this when we first started them up, but we’re still under 3 hours total run
time.
It was coming from the
injector pump, and I was hoping I could just find a loose fitting somewhere to
tighten. But, it was coming through a pinhole in a diaphragm that protrudes
from the block side of the pump. It’s about 2 or 3 inches in diameter and
is in the center of the 2nd photo below. I talked to the folks
at Seattle Injector, and they said on this particular model pump (model
3062F541) this device, a fuel pressure damper, regulates the fuel to prevent
smoke when accelerating. They said it would run without it if it were
removed and the hole plugged, but that it would likely cause the engine to
“hunt” and not hold a steady rpm if it were missing. The diaphragm inside
the device has failed, causing the fuel to leak through the pinhole.
Actually, it spurts out in pulses with the pump’s rotation.
I
wrote to SeaMaster Marine in Florida with pictures and a video of the leak, and
Ron said to buy the part at Seattle Injector and he would reimburse me. I did and he did. The part, pictured above, was a little
awkward to remove and replace, as one can only get one finger on it at a
time. It went quicker than I
anticipated, however, and once replaced the engine ran fine and the leak was
gone.
Speaking
of leaks, we also had a leak on the port engine - this one with coolant. I had noticed some coolant leaking earlier
around the overflow hose under the expansion tank cap, and assumed it was
because we didn't have a clamp holding that hose on. I had put a small clamp on it while replacing
the turbocharger, but the next time I ran the engine it was still leaking. Closer examination revealed that the neck
coming out of the expansion tank was cracked and that's where it was
leaking. The cooling system was not
pressurizing or sending overflow coolant to the recovery bottle - it was just
leaking out, running to the underside of the expansion tank and then dripping
down onto the serpentine belt, which in turn sprayed it out across the aisle
between the
engines. I drained two or three gallons of coolant
from the engine and removed the tank.
With the tank in the trunk
I headed north on Hwy 99 trying to find a shop that could repair it or put on a
new neck, either brazing or pressing on – not quite sure how it’s supposed to
be connected. I had remembered a small radiator shop north of Lynnwood
because it had a sign that read "The best place to take a leak!" Of course that was several years ago, and now
they were nowhere to be found. I did get
the addresses of a few radiator shops in that general direction before I left
on my quest, but quickly discovered that most places that now advertise being a
radiator repair facility merely remove plastic radiators from cars and replace
them. A couple places recommended Performance Radiator in Everett, but
when I called them, they said they’d send it to their shop in Tacoma to evaluate.
Finally I was sent to Greenwood Radiator in North Seattle, where they’ll heat
it up, remove the neck and see if it’s reusable or if it needs a new one.
By
now Ray was well on the road to recovery, and he and I went back to Greenwood
Radiator the next morning, with the thought that if they weren’t going to get
to it for another day or two we’d just buy the new neck and do our own
repair. We showed up about 10 o’clock in the morning and it was already
repaired. He had cut out the old piece, ground off a bunch of pitted
metal around it, welded on the new neck with overflow tube and pressure tested
it. All for $45 in labor, plus a few more bucks for the neck and
tax. What a deal! We took it to the boat, bolted it on, slapped a
little paint on it, filled it up and ran the engines up to operating
temperature. Works great – another problem solved!
I
had written to Seamaster Marine about this as well, and although they said the
tank was fine during their dyno test they had offered to do whatever I thought
was right. From the looks of the crack
in the neck, I'm pretty sure it got stepped on either in transit or by someone
here in the months of preparation before our first start. I told Ron at Seamaster not to worry about it - that I'd save the good will for a more expensive future problem that we both hoped would never occur.