Our choices as to fixing it seemed to be to either machine the housing down to a flat surface, or replace the turbocharger. Mechanically, the turbocharger was fine, spinning freely with no bearing play at all, but I wasn’t too keen on the machining, as it appeared that the pitting was caused by water damage in a previous lifetime for this unit and there may be other issues inside waiting for us. Also, the amount we’d have to take off to square it up would reduce the bolt hole depth and thus weaken the connection to the riser. I sent photos to Seamaster Marine in Florida, where we purchased the engines, and they agreed to send up another turbocharger, which should be on its way today. We’ve removed this one from the boat and will pack it up and send it back. Unlike the turbochargers on the old Perkins engines, these units are water cooled, so we had to drain all the coolant from the port engine – we’ll be going through the thermostat exercise again.
So,
our initial sea trial has been delayed by at least a week while we wait for the
new turbocharger. That’s when we’ll find out if we can reach the engines’
rated maximum rpm of 2600. According to some online calculators we should
be able to, or at least come close. This will tell us if our props are
the right size. If we are substantially below max rpm, we may have to
have the props re-pitched – otherwise the engines could be overloaded even at
the lower rpms.
We
did get the roof panel we removed bolted into place so it wouldn’t go flying
off as we headed into the wind. Patching the saw kerfs will come later,
so our sea trial will be on a dry day – perhaps another unreasonable
requirement this time of year. Irv from Gallery Marine warned us that we
should expect smoke and burning smells from the paint on the engines as
manifolds and other various parts come up to operating temperatures. He
told us that they usually don’t even take customers along on an initial sea
trial run for this reason, adding “whatever you do, don’t bring the womenfolk
along – they always freak out.”
The
turbocharger weighs close to 50 pounds, so Ray made a shipping box for it from
some scrap pieces of plywood and 2x2s.
I'd say this box is pretty well engineered!
Erin
and I did some weekend work at the boat while waiting for our replacement
turbocharger. Our above average rainfall has made an appreciable change
to the lake level, as the boat has risen well over a foot over the last month
or two. So, we brought along the steps that we’ve been bringing home each
fall.
For the most part it worked, except for a drip in one corner.
So now we’ll at least look somewhat respectable from a distance when we head out into the lake for sea trials once our replacement
turbocharger arrives. Ray and I recently reconnected the lines to the air
horns, so at Erin’s urging, of course, I gave her a brief demo, being careful
to not signal the University Bridge to open.
Our
replacement turbocharger arrived on 3/29, but on that same day Chief Engineer
Ray was ill, and eventually was checked into the hospital for abdominal surgery
to repair a hernia as well as some strangulated bowel. The good news is that Ray has since
recovered, and we delayed any sea trial attempt until he was ready to participate,
hear the roar of the exhaust and smell the paint burning off the manifolds as
we accelerate to maximum rpm out in Lake Washington. It’s a big step in
the fruition of our labors over the past several months.
I
was pretty sure Ray wouldn’t be interested in hefting the 45 lb. turbocharger
anytime soon, so while he was recovering I got it bolted into place. New
gaskets came with it as well, and I added some high-temp silicone sealer
between the manifold and turbo, and some lithium grease to the exhaust
port. Once the turbocharger was securely
in place I could add the coolant back into the engine. Rather than mess with a
funnel and trying to clumsily pour from the bucket into the smaller bottles or
the expansion tank, I found some hose and started a siphon to fill the
engine. It worked great and I poured the individual jugs of coolant into
the bucket as
the level was siphoned
down. You can see the reservoir bottle bolted into place and yes, the
overflow hose has since been connected to it.
With
the exhaust and raw water systems reconnected, and coolant back in the engine I
started it up for a test. No exhaust leaks, and enough coolant found its
way into some additional areas that I could add nearly another gallon to top it
up.
Diesel
engines need to be able to achieve their maximum rated rpm at wide open
throttle under load to assure that they are not overloaded throughout their
working range. In actual use, we will seldom, probably never, run at the
maximum rpm, but if the engines are unable reach their maximum, in this case
2600 rpm, it will mean the boat is “over-propped” – the diameter and pitch of
the propellers take too big of a bite for the engine to handle properly (no pun
intended). While we could easily cruise at our usual 8 or 9 knots even
when over-propped, it could be likened to driving around in a stick shift car
in high gear at 15 or 20 mph – you can do it but it’s not good for the engine
to be lugged down like that. We’ve used calculators available online that
indicate we are pretty close to being just fine based on our horsepower, boat
weight, length, beam, reduction gear ratio, and diameter and pitch of the
propellers. But the real test will be when we head out on the water to
see how she performs. If we end up topping out a couple hundred rpm short
of max, then when we haul the boat out for maintenance we’ll take the props to
the prop shop and tell them we need a couple hundred more rpm. They’ll
know how much pitch needs to be taken out if that’s the case.
With
the engines pretty much ready for sea trials, I decided to focus on some other
chores while Ray recovered from his surgery. As part of opening up the
hatch in the roof we had to cut through some wires as well as the copper tubing
to the air horns. The wires were to the stereo speakers further ahead in
the roof. They are shielded pairs, and required some nipping to get to the individual wires inside. They’ll be
rejoined with compression splices. Ray and I had already reconnected the
horns using plastic tubing, but the tubes needed to be secured so they wouldn’t
cause a bump once we put the headliner back into place.
Speaking
of leaks, we also had a leak on the port engine - this one with coolant. I had noticed some coolant leaking earlier
around the overflow hose under the expansion tank cap, and assumed it was
because we didn't have a clamp holding that hose on. I had put a small clamp on it while replacing
the turbocharger, but the next time I ran the engine it was still leaking. Closer examination revealed that the neck
coming out of the expansion tank was cracked and that's where it was
leaking. The cooling system was not
pressurizing or sending overflow coolant to the recovery bottle - it was just
leaking out, running to the underside of the expansion tank and then dripping
down onto the serpentine belt, which in turn sprayed it out across the aisle
between the
engines. I drained two or three gallons of coolant
from the engine and removed the tank.
By
now Ray was well on the road to recovery, and he and I went back to Greenwood
Radiator the next morning, with the thought that if they weren’t going to get
to it for another day or two we’d just buy the new neck and do our own
repair. We showed up about 10 o’clock in the morning and it was already
repaired. He had cut out the old piece, ground off a bunch of pitted
metal around it, welded on the new neck with overflow tube and pressure tested
it. All for $45 in labor, plus a few more bucks for the neck and
tax. What a deal! We took it to the boat, bolted it on, slapped a
little paint on it, filled it up and ran the engines up to operating
temperature. Works great – another problem solved!
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